AD Amdt-39-9504
Applicability
| Type | Manufacturer | Model | Details |
|---|---|---|---|
| aircraft | Beech | Model 400, 400A, and MU-300-10 | Airworthiness Directives; Beech Model 400, 400A, and MU-300-10 Airplanes |
Unsafe Condition
Incomplete latching of the existing adjustment mechanism and cracked reinforcement assemblies could result in sudden shifting of a flightcrew seat.
AI-generated summary from the source AD text. Verify against the official source before acting.
Required Actions
Install an improved adjustment mechanism on the flightcrew seats and replace existing aluminum seat reinforcement assemblies with steel assemblies.
AI-generated summary from the source AD text. Verify against the official source before acting.
Compliance Time
Before further flight
AI-generated summary from the source AD text. Verify against the official source before acting.
Affected Aircraft
Beech Model 400, 400A, and MU-300-10 airplanes
AI-generated summary from the source AD text. Verify against the official source before acting.
Source: Official FAA Source ↗
Retrieved: Apr 6, 2026
Rights: U.S. Government Public Domain
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