AD Amdt-39-18007

Recurring final rule
Data completeness: 70%

Airworthiness Directives; Dowty Propellers Constant Speed Propellers

AD Number
Amdt-39-18007
Status
final_rule
Effective Date
Product Category
propeller
Docket
Docket No. FAA-2009-0776
FR Citation
79 FR 71300

Unsafe Condition

Failure of the propeller de-ice bus bar due to friction or contact between the bus bar and the backplate assembly, consequent intermittent short circuit, and possible double generator failure.

AI-generated summary from the source AD text. Verify against the official source before acting.

Required Actions

Apply sealant between the bus bar assemblies and the backplate assembly for R408/6-123-F/17 model propellers with LRU S/N below DAP0347 within specified compliance times. Re-apply sealant every 10,500 flight hours for R408/6-123-F/17 model propellers with LRU S/N below DAP0927.

AI-generated summary from the source AD text. Verify against the official source before acting.

Compliance Time

Within 5,000 flight-hours after September 27, 2010, or within 100 flight-hours after the effective date of this AD, whichever occurs later.

AI-generated summary from the source AD text. Verify against the official source before acting.

Affected Aircraft

Dowty Propellers R408/6-123-F/17 model propellers with a hub, actuator, and backplate assembly LRU serial number (S/N) below DAP0927.

AI-generated summary from the source AD text. Verify against the official source before acting.

Source: Official FAA Source ↗

Retrieved: Apr 6, 2026

Rights: U.S. Government Public Domain

This site is not affiliated with or endorsed by the FAA. Always verify with official sources.

View Official Source ↗