AD 88-07-08

final rule
Data completeness: 70%

GENERAL ELECTRIC Model CT7-5A, -5A1, and -5A2 Engines

AD Number
88-07-08
Status
final_rule
Effective Date
Product Category
engine
Docket
Unknown
FR Citation
This information is not available.

Applicability

TypeManufacturerModelDetails
engine General Electric Company CT7-5A2 GENERAL ELECTRIC Model CT7-5A, -5A1, and -5A2 Engines

Unsafe Condition

Power turbine overspeed resulting in an uncontained failure or adverse aircraft yaw due to reaction of the fuel control to an erroneous PT speed signal during ground operation with the bottoming governor enabled.

AI-generated summary from the source AD text. Verify against the official source before acting.

Required Actions

Remove propeller overspeed governor (Dowty Rotol P/N 661001001) and replace with P/N 661001002 per DR SB SF340-61-11. Install cable GE P/N 6068T47P01 between OSG and hydromechanical unit per GE SB 74-09. Install engine BG deactivation switches (Saab Mod Kit SF340-76-018-01) per Saab SB SF340-76-018. Remove BG disabling procedures from AFM per AD 86-10-51 and discontinue those procedures. Ferrying allowed under FAR 21.197/199. Equivalent compliance may be approved.

AI-generated summary from the source AD text. Verify against the official source before acting.

Compliance Time

no later than May 16, 1988

AI-generated summary from the source AD text. Verify against the official source before acting.

Affected Aircraft

General Electric CT7-5A, -5A1, and -5A2 engines installed in Saab-Fairchild SF340A aircraft

AI-generated summary from the source AD text. Verify against the official source before acting.

Source: Official FAA Source ↗

Retrieved: Apr 8, 2026

Rights: U.S. Government Public Domain

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