AD 51-01-01

final rule
Data completeness: 60%

Airworthiness Directives; DOUGLAS All DC-6 Aircraft

AD Number
51-01-01
Status
final_rule
Effective Date
Product Category
aircraft
Docket
Unknown
FR Citation
This information is not available.

Applicability

TypeManufacturerModelDetails
aircraft The Boeing Company DC-6 Airworthiness Directives; DOUGLAS All DC-6 Aircraft
aircraft The Boeing Company DC-6A Airworthiness Directives; DOUGLAS All DC-6 Aircraft
aircraft The Boeing Company DC-6B Airworthiness Directives; DOUGLAS All DC-6 Aircraft

Unsafe Condition

Broken studs at the front spar lower and upper fittings at wing joint Station 421 and cracks in lower and upper forward front spar fittings (P/N 4332884, -1, 4332885, -1) approximately 2 inches outboard of fitting face.

AI-generated summary from the source AD text. Verify against the official source before acting.

Required Actions

Inspect for broken studs and cracks at specified fittings every 300 flight hours. Replace broken studs with parts having threads rolled after heat treat, install bolts with threads rolled after heat treat at center spar, and replace fittings with newly designed heavier P/N 4397872/-1 and 4397873/-1. Allow temporary replacement with old design fittings until 8,000 hours service, then spotface new fittings. Continue inspections until permanent replacements are done by January 1, 1952.

AI-generated summary from the source AD text. Verify against the official source before acting.

Compliance Time

Not later than January 1, 1952

AI-generated summary from the source AD text. Verify against the official source before acting.

Affected Aircraft

Douglas DC-6, DC-6A, DC-6B aircraft (all serial numbers)

AI-generated summary from the source AD text. Verify against the official source before acting.

Source: Official FAA Source ↗

Retrieved: Apr 8, 2026

Rights: U.S. Government Public Domain

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